I would think thats detonation.
Sure the plug looks a little white and head/piston a bit clean, but IMO, it doesn't look like bat detonation if it were.
What looks more like detonation is the "pitted" or area by the exhaust port. Those big "chunks" on the edge of the piston don't seem to go with that story.
Then again, maybe the knock sensor was telling it to retard the timing and hence the shitty running.
Problem here is where is the extra air coming from? Bad gas ending up with clogged jets? Engine pressure tests ok so the seals on the crank should be good.
Temperature was warmer so more oxygen = leaner, but the other piston looks nothing like a lean jetting =)
Noticed the exhaust port pitting when really zoomed in so maybe the pipe flange is leaking a bit? The one bolt backs out, but the others remain good. I snugged the bolt up for the pressure test so maybe when it was loose it was seeping air in?
No crack in y-pipe with pressure test on Y-single port plugged.
Can somebody confirm this is detonation and not a hungry engine?
I agree with MOFOREV telling your center crank bearing is pooched.srry man ,my thoughts anyway you can read my article in another thread similar stuff.mY MOTOR HAD 3300 hard MILES when it started acting up.I didnt have deto like that but i had bad scoring on cylinder walls(mag side) and such,not real bad but bad enough..that when the clam shells were knocked apart the center bearing was just F'D......yOU SHOULD HAVE CHECKED YOUR CRANK RUNOUT TO BOOT before taking jug off.
Kluber Isoflex Topas NB 52** Snowmobile Grease
Hum... I'll have to double check but that appears to be the same stuff...